Author Archive: wae

Paint sucks.

I was lamenting the primer/sand/primer/sand/primer/sand/base/sand/base/sand/base/sand/clear/sand/clear/sand/polish process to a co-worker and he asked me why I was bothering to paint it.  “Just wrap it”, he said.  My immediate thought was that I could’t vinyl wrap it because…  er..  well…  uhm..  heeeeyyyyy…  why can’t I vinyl wrap it!?

I ordered a 5’x2′ sheet of 3M 1080 in Gloss Blue Metallic, got some knifeless tape, and then went to Meijer for a can of denatured alcohol, some silicon kitchen spatulas to use as squeegees, a bottle of propane, some good scissors, and got to work.

I decided to start off easy, so I tried the gas door.  I had already sanded and primered it, but my first lesson was that any little imperfection in or on the surface will be VERY obvious in the vinyl.  The gas door had a couple tiny little particles of paint on it that caused some really ugly bumps all over the surface, so I pulled the vinyl off, and used a razor blade to smooth the surface of the door.  Once it was smooth, I pulled out a new bit of vinyl and with a little stretching, squeegee-ing, and some heat from the torch, I got this:

I am very impressed with how nice it winds up looking!  It has a deepness and uniformity to the color which would have been very difficult for me to achieve with paint.  It also doesn’t want to chip very easily, but it does seem to be easy to scratch — the vinyl wound up having a couple scratches in it as it came off the roll.

My next attempt was the lid for one of the side bags.  I tried doing it as one piece, all the way around, and I just can’t get the vinyl to shrink enough around the corners.  On one side, I managed to burn a hole through and on the other, it just won’t un-wrinkle.  I’m going to peel back some of that vinyl and use the knifeless tape to put a seam in to finish that one without wasting the vinyl that’s already on (or at least most of it) and then I’ll do the other side making sure that I put the seam on the side that faces towards the frame.  Future parts will need to be done similarly to avoid that mess.

I’m not entirely sure how much of this stuff I’ll wind up needing, but I ordered another roll 30’x5′ today as well as a 1’x5′ roll of carbon fiber pattern vinyl for some of smaller trim bits.  I’m thinking that maybe the insides of the forward-facing vents for the lower front covers and for the bottom sections of the left and right side panels.  It goes on so easily, though, that I may make liberal use of it to help improve the overall look of the bike.  Right now I’m thinking that I might be able to find a vinyl that would work well on the inside of the front fairing (the dashboard?) to make it look like it isn’t 30 years old.

So far, so good!  Looks like I’ll be able to ride this thing soon, if I can keep this up.

Getting Ready for RallyX 2015 and Planning for the Future

Good news/bad news:  I’ve been doing more work on the car than I have been updating my build journal.

After the last axle replacement, the transmission was just hemorrhaging Synchromesh fluid.  I was hoping that the problem was just the seal, but in the process of trying to swap that out, I managed to pull the axle out of the trans without applying any real pressure at all.

Taking everything apart again, I found that the hole in the OBX LSD is just not bored out right.  I finally wound up grinding off about an eighth of an inch from the end of the axle and that seems to have gotten the job done — the axle is seated firmly and does not leak.

I also put on a 3″ stainless downpipe that was bought from eBay.  There’s still an exhaust leak somewhere that I can hear, but I haven’t had a chance to dig in and find out exactly where it’s coming from.

During the process of working on the axle/transmission, I discovered that my intake tract made of steel exhaust pipe has been rubbing against the brake lines by the master cylinder.  In order to hold that steady, I’ve made a bracket from some small angle iron and a little bit of sheet.  That will bolt to the valve cover and then I’ll rig up a way to connect the pipe to the bracket to hold it steady.  I’ve also put another bend in the intake to try to scavenge some colder air.  The bracket will also secure wiring and hold the catch can for the breather side of the PCV system.

In bigger news….  While I was at the junkyard on a separate mission, I stumbled across a PT Cruiser with the “turbo-light” 180hp 2.4L turbo.  For about $250, I was able to score the oil pan, block, head, intake manifold, exhaust manifold, throttle body, turbo, all the water and oil lines, accessory brackets, and the hot-side and cold-side charge piping.  I’m going to put it on a stand, rebuild it, and then drop it in.  No rush on that project right now, though.

Shooting Primer and Base Coat

I’ve got my PVC-and-sheeting paint booth set up in the garage and have started getting things colorized finally.  I’ve already gone through three tall cans of primer and there’s plenty left to do, so that activity got delayed for a while.  In the meantime, I decided to go ahead and try shooting some color onto the sides of the faux tank.  The close-up pictures make it look really turquoise, but it’s a much darker blue than that.  It needs a couple more coats before I’m ready to consider it ready for wet sanding and then I’ll hit it with clear, but so far, I’m pretty happy with how it’s turning out.  Not bad for some rattlecans.

Either Painting has Started, or I’ve Captured E.T.

With rising temps getting the inside of the garage to over 50 degrees, I got the paint booth set up in the garage and got started.  Due to a late basketball game tonight, I wasn’t able to get very far, but I have a couple coats of primer on a handful of panels and it’s starting to look pretty good.

Items for Sale

« of 2 »

A Long Awaited Update

Most of my time in the garage over the summer was spent putting transmissions in the Neon, and as a result the motorcycle side of the garage has turned into a horror show of disorganization and disaster.  I started organizing things a little bit a couple weeks ago and finally got the Goldwing project unearthed so I can try to get this thing wrapped up finally.

Two nights ago, I had the bike cleared out and all the bodywork set aside and identified (except for the left side cover, but more on that later) and was wrapping up mainly due to the dust and dirt aggravating my allergies.  As my last step, I decided to just sit on the bike and enjoy it for a minute, but once I did that, I couldn’t leave it alone — I had to turn the key to see if there was any juice left in the battery.  Sure enough, all the lights came on so I turned the choke, flipped the run switch on, and hit the starter.  After sitting out there in the garage for the last four or six months without being touched, it started up without any hesitation.  Go Honda.

Anyway, last night I went out to find the left cover since that’s the last bit of bodywork that I need to prep.  Thanks to my efforts in digging out the crap, I was able to find it in about a minute and a half.  I sanded it down and used a bit of PVC cement to seal up the cracks.  It’s not finished yet — I need to fill in the larger crack a bit, and then I have to find a way to clamp one of the smaller cracks to hold the plastic together, but I should be able to get that wrapped up tonight and then I can start painting soon!

 

Leaks are Mostly Fixed. And a New Axle. Again.

It turns out that I had way more motivation than I thought the other night!  Not only did I get the pan drilled, but I swapped the pans, got the steel-braided hose cut and built, tightened everything up, and filled it with oil.  A quick test drive showed a small leak from the blank plug on the oil filter sandwich adapter, but after torquing that down real well, I don’t see any leaks.

I was getting a leak from the left side, coming off the bottom of the transaxle, but I couldn’t really tell what it was.  I didn’t do anything about it immediately because I knew that the axle was bad and needed to be replaced — during the trans swap, I tore the boot and despite sealing it up with some silicone, I think the 860 mile trip through the rain got plenty of junk in and all the grease out.  No big deal, though:  I went ahead and exchanged the busted axle at O’Reilly and swapped it out tonight.  Took me just under an hour, but that included trying to find my stupid tire iron (left it in the van) and boogering up an axle seal.  I think the original axle seal was damaged when I put it in after the OBX went in and the leak on the left side was Synchromesh.  Upon swapping out the seal, I managed to bend up the first one I put in, so I pulled it out and put my last spare in — I think this one went in okay.

I also found that I had to swap out the c-clip with the one that I had rounded off in order to get the axle to seat.  One of my big worries with doing that originally was that I wouldn’t be able to remove the axle at all, but I was fortunate in that it took some effort, but nothing extraordinary to remove the bad axle from the diff.

Next up, I need to get it out and give it some test driving, but I’d rather do that in daylight.  Should be good to go for the first RallyCross of the WOR season this coming weekend, though!

Back to the Oil Leak

The astute observer will notice through this project that the car has always had an oil leak of some sort.  While it has been a little better recently, there’s still oil escaping the car.  There have been two main sources of the oil so far:  The turbo lines under high pressure and the valve cover vent tube under hard cornering.  The valve cover problem is not a real big deal to me and can be fixed with a second catch can and/or installing a baffle of some sort on the valve cover.  The turbo oil line problem, however, is a bit more concerning.  This has manifested itself in the past when the car is super cold — as in, below freezing — and the oil pressure is very high.  I actually filled the cabin with oil smoke once because the oil was spraying out of the oil line and onto the exhaust.

While at Nationals, the car started to hemorrhage oil at a much faster rate.  The drive back to Cleveland consumed about a gallon and a half of oil, all of it spraying out the bottom of the car.  The oil pressure sender also lost its little thumbscrew that held one of the wires on, so we couldn’t even really monitor the oil pressure.

Before I put the transmission in, I had bought the AN plumbing and braided hose to re-do the oil lines, but I didn’t have a chance to get that done before nationals.  So I went ahead and pulled the old lines off and got to work getting them replaced.  When I pulled the old feed line off, I put the slightest bit of pressure on it and it wound up snapping in half, so that was a ticking time bomb and the source of all that oil.  The new lines are coming together nicely:  The feed line is already installed with plain braided stainless line with angled AN fittings and an AN to NPT adapter at each end.  The drain line is in progress with the tube-to-AN adapter installed and the tube re-installed to the turbo.  Rather than use more copper RTV or the stock SRT-4 gasket, I got the gasket for an old Dodge Stealth from the Dodge dealer since it seems a little sturdier.  I also picked up an oil pan at the junk yard so that I can start over and put the return bung in without using any JB Weld.

I needed to run out and get the right sized hole saw, but I did mock up the return line last night.  The hose end is angled as is the bulkhead AN fitting, so it looks like once I get the right oil pan in there, the return hose will be a very short, very straight shot right into the oil pan with no chance of interference with the passenger-side axle.

Tonight, I hope to get the new oil pan drilled and install the AN fitting.  I hope to also be able to get that new oil pan installed at a minimum, but we’ll see how much motivation I wind up with.

A bunch of updates

Since my last update, I ran the car at the GLDIV National Challenge and the Rallycross Nationals in Nebraska and it has been something of a wild ride.

In reviewing my previous post, the keen observer will notice that I destroyed another transmission.  Basically, my assembly method of just torquing the case halves together was pretty much the dumbest thing I could do.  By the time the car came home from the divisional, the transmission was completely thrashed.  Teeth missing,bearing bits rolling around, the whole deal.  The divisional itself was a challenge:  I broke a CV in the morning of day 1 and then had a ground wire come loose in the afternoon which absolutely killed my times and put me in third place.  I was also doing a lot of one-wheel action and through the pictures that were taken realized that it was a lot worse than I thought.  Nationals were going to require a lot of work.

For the transmission, I found someone in Columbus who had a trans for $75 that was already removed from a car.  From Modern Performance, I got an Ed Peters modified OBX limited slip.  I also got a set of Koni STR.T struts for the rear.  Tim helped me get the transmission put together since he is much better at those fiddley things than I am.  The LSD came with new bearings and races, and I sourced new ring gear bolts from the Internet.  I found that the axle didn’t want to seat all the way on the driver side, so I ground down the retaining ring to put some curve on the edge and was able to get it to slam into place.  I also went ahead and put the power steering back on the car.

For the rear struts, I got some really big and stiff bump stops and put them in to try to prevent oscillation. 

The wiring was fixed and I added a ground strap to the engine.

The combination of power steering and the limited slip is amazing!  There is all sorts of additional grip and power that I didn’t have before.  And with the rear end being so much stiffer, the car is much more controlled.

In the end, I was 7 out of 14 in MF, so not a great result, but the car made it through the event and then made an 850+ mile journey to Cleveland because I was trailering Pete’s car since it wasn’t in any shape to be driven back.

More Sanding

Still no pictures to add, but I’ve started using PVC cement as a filler/repairer and it seems to be working well. I scraped and peeled the 3M stuff off and then hit the surface with more sandpaper and acetone to encourage adhesion before applying the cement to the plastic. It has to go on in fairly thin layers, otherwise you get a ton of air bubbles and pinholes, but through a regimen of application, sanding, application, sanding, and so on, the plastic panels are smoothing out and taking shape. At this point, one of the saddle bag lids, the main tank cover, the side fairings, the right side cover, the lower cowl bit, the trunk lid, and the trunk trim bit are all ready for primer. The main fairing is going to stay on the bike and get painted in place, so I’m fixing to do that last. The remaining bits still have some build-up and sand-down work to be done before they’re ready to have a final wet-sand to be ready for primer. I have tried putting the PVC cement on some of the panels and giving them some pretty serious flex and I haven’t seen any problems with the fill cracking, stressing, delaminating, or any other issues, so I’m pretty hopeful that this will wind up looking good. From what I can tell, the PVC cement is basically PVC fillings suspended in MEK and once the MEK evaporates, the PVC hardens and just becomes plastic. By sanding down the paint and using a little acetone to soften up the underlying plastic, the PVC and the ABS should be bonding pretty tightly.

While the PVC was drying last night, I took the opportunity to get some PVC piping that I had left over to build a frame for painting the parts. It’s fairly small diameter pipe (1.5″, I think?) and I basically just made a quick bar-on-a-stand out of it so that I can use bent-up wire hangers to suspend the plastic body bits in order to be able to get them well covered. I’ve also started covering the various bolt-holes in the panels with duct tape from the un-painted side and will work on getting them masked the rest of the way as Paint Day get closer.